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[Date Prev][Date Next][Date Index] UNC Carolina Air Care - Non-injury incidentDate: Dec 18, 2007 1900 EST Program: UNC Carolina Air Care UNC Hospitals 101 Manning Drive Chapel Hill, NC 27514 Type: BK117 Tail #: 118NC Operator/Vendor: CJ / Air Methods Weather: Not a factor Team: Pilot, Flight Nurse, Fight Paramedic. No injuries reported. No patient. Description: Pilot shift change at 1830. Information passed from day pilot to night pilot about aircraft having a brief slowing, drop in power with quick recovery on three take off's from that day. After third event the pilot discussed this event with a mechanic. There was an inspection of the aircraft with no specific issue identified. The aircraft did a retun take off from the main base back to it's satellite base. Night pilot on duty at 1830 with a mission request received. Aircraft lifted, shortly after take off the pilot made a decsion to put the aircraft in an aproach position to determin if the events described by the day pilot may reoccur. If any issues the pilot would abort the mission and take the aircraft off line. The aircraft had an unexpected response to the maneuver going into a 30 degree pitch. The pilot was able to make recovery and right the aircraft. The mission was aborted. The aircraft returned to base without further incident. Additional Info: The aircraft had returned from an extensive PM service 4 day's previously. The aircraft was flown from Pittsburgh PA to Fayettevill NC by a pilot who routinely works with the other aircraft and is not familiar with this aircraft. The next pilot to fly the aircraft makes a statement at the end of his shift to the oncoming crew that there is something different about the way the aircraft is flying. The next comment comes from a pilot who has a head cold, notes there is a difference in the handeling of the aircraft but attributes this to his cold effecting his senses. The following night this pilot receives the shift change brief about the 3 episodes and later states that he felt a sense of uneasyness after hearing the day pilot's comments but did not feel he had anything concrete to take the aircraft off line. This lead to his making the decision to put the aircraft in an approach position befor getting to far from base on their mission at 1900. After the event, the aircraft was evaluated by the mechanics, the "porpoising" effect was reproduced. The aircraft was trucked to Pittsburgh. A hydraulic pack which had been replaced during it's previous PM service was replaced again. The aircraft continued to have issues. Additional evaluation was completed. The aircraft was found to have a bearing block on top of the main gear box that was "going bad". This was replaced, there have been no further issues. The aircraft has been released back to the line and is expected back in NC within the next day or two Source: Maggie O'Donnell Program Manager =-=-=-=-=-=-=-=-=-=-=-=-=-=-=-=-=-=-=-=-=-=-=-=-=-=-=-=-= The CONCERN network shares verified information to alert medical transport programs when an accident / incident has occurred. Please share the above information with your program staff. If you have further questions, please contact the CONCERN Coordinator, David Kearns at 800 525 3712 or email: coordinator@concern-network.org. Copyright 2007 ASTNA
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